Trever the rever Posted August 7, 2018 Report Share Posted August 7, 2018 I have the eternal TR problem of the horn going off intermittently on its own accord. I replaced my (1972) standard steering about 20 years ago with what I led to believe was an earlier type with a thin leather rim and separate deeper boss which necessitated the longer push connection. My column was also in the most upward position until last year which I had grown use to. However my local garage lowered it which was good. The horn issue to be honest was there before and after the step change. I believe its the boss shorting out on the horn ring in a random manner. I have recently tried to insulate as much of the exposed parts to avoid connection, which works for a while but eventually it breaks down I imagine due to the rotation of the wheel. I can see if the inner column is raised by 1-2 mm this would move the boss away from the horn ring and I hope solve the problem. Please could I receive advice how this can be done. Is it simply from the connection clamp under the bonnet, or is there something more intricate on the column under the dash? many thanks Trevor Quote Link to post Share on other sites
RogerH Posted August 7, 2018 Report Share Posted August 7, 2018 Hi TRev, quite often the steering wheel hub is pushed too far forward and rubs on the column/control head. Slacken off steering clamps in the engine bay and pull steering wheel rearwards, see pic Roger Quote Link to post Share on other sites
Trever the rever Posted August 7, 2018 Author Report Share Posted August 7, 2018 Perfect Roger I'm hoping this will work, aiming for tonight when its cooler! Cheers Trevor Quote Link to post Share on other sites
Mike C Posted August 7, 2018 Report Share Posted August 7, 2018 +1 for Roger plus make sure the brass ring and carbon electrode's track are concentric and aligned properly. Quote Link to post Share on other sites
openroad Posted August 7, 2018 Report Share Posted August 7, 2018 I had this happening when turning right, very embarrassing at Blyton on the track !! I hadnt fitted the black slip ring, cable insulator, properly. It has to go into its slots firmly, mine was loose. Good luck, Conrad. Quote Link to post Share on other sites
Trever the rever Posted August 7, 2018 Author Report Share Posted August 7, 2018 Adjustments made this afternoon, please see photos, about 1.5 mm (ish). Test drive okay after cleaning up the red insulation tape beneath the boss! Few drives planned this month, so lets hope that's done the trick. Thanks for the advice. Regards TRevor Quote Link to post Share on other sites
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