Jump to content

PaulR

Registered User
  • Content Count

    100
  • Joined

  • Last visited

Posts posted by PaulR

  1. Hi All

    Thx for the replies

    The car is a 4 not 4a so has solid axle

    Hopefully over enthusiastic grease gun as otherwise sounds a bit of a 'mare

    Only appeared on the off side

    Have cleaned it all out so will give her a run on DiD and check after

  2. Was carrying out a few checks prior to Drive It Day and found quite a large quantity of grease (see photo, although I have wiped some away) over the brake shoes. Can only assume it has come from the hub but never having taken the rear hub apart I don't know where the seals would be. Anybody got any ideas where it has come from & what I need to do?

    Thx in advance

    Paul

    20240414_141942.jpg

  3. Update

    Finally success

    The door seal rubber was preventing the door closing sufficiently for the second 'clack'

    By moving the door forward on the hinges it reduced the pressure on the seal & hey presto

    Thx to all for their comments

  4. Hi All

    Thx for your input

    The door alignment is fine. It will close in an acceptable position

    The issue is that the cog/striker plate won't hold it in that position

    I'm going to try and get into the rotary lock mechanism and see what I find

    Paul

  5. Another afternoon spent trying to improve the closing of the door without success

    Reading Efuentes post he talks about 2 clacks. I can only get one no matter where the striker is positioned 

    There does seem to be some slack in the cog on the door, could this be the reason and is there anything that can be done about it

    Hers's hoping

    Paul

  6. Due to quite a lot of movement in all of them I decided to ream & replace the door pins in all 4 door hinges. This worked very well, Hoorah!!

    However on refitting the doors I cannot now get them to close sufficiently. (see photos) 

    This applies to both doors

    The Door Lock Striker is at it's most inboard position. I have also tried them at the most outboard position in the hope that the toothed wheel on the door may click twice, no dice!!

    I have tried adjusting the hinges in the door & A post but can't get it right

    Am I missing a trick & if not any suggestions for a door 'guru' in West Sussex

    many Thx

    Paul

    20210325_140821.jpg

    20210325_140854.jpg

    20210325_140914.jpg

  7. As the rest of the wing is in good shape I like David's idea of cutting the front off an existing wing

    Dave I hope that I have sent you a message through the forum, although I have never one that before so hope you get it

  8. The current situation provides an opportunity to re-visit my 14 year old  fibreglass & filler repair to the front of my o/s front wing. It held up really well & I had forgotten how bad the wing was - see photos. Now wanting to do a repair in metal rather than filler. Does anyone make a repair panel for this area & if not has anyone got any suggestions

    Many Thx in advance

    Paul

    20201109_150808.jpg

    20201109_150846.jpg

    20201109_150705.jpg

  9. Having got an alternator & thin belt conversion my ammeter is redundant. I would like to convert it into a clock keeping the Jaeger logo to match. Has anyone done this or got any suggestions? I'm happy to scan & print the logo on a black background but not sure where top find a mechanism. Thx

  10. I recently posted ( 3 weeks ago) how the ballast resistor on my Lumenition ignition had failed & I replaced the coil with a Lucas gold one and did away with the resistor

    All was fine until today, when she died. After a bit of diagnostics the lucas coil has failed (It wasn't that old). I'm now thinking that I may have too high an output form the alternator that has burnt out the ballast resistor and now a perfectly good coil.

    Any suggestions as to my next step please.

  11. Hi

    A very nice AA man got me on my way again today by diagnosing that the 1.5 ohm ballast resistor on my magnatronic ignition had failed. I had a spare lucas coil which we fitted, by passing the resistor and all seems fine. I was never a fan of the bloody great resistor anyway so am wondering if anyone has any views on running on the current setup.

  12. I'm with Roger on his logic but can't think how changing the rear shoes would affect the front brakes

    I also agree with Stuart that a seized o/s calliper would explain the results but what would cause a calliper to seize that had been performing perfectly?

  13. Always had quite a lot of travel in the brake pedal so recently replaced the rear shoes. This seemed to make things much better

    Was out for a run in the sun yesterday when the brake pedal became very firm with very little travel and a huge pull to left when applied.

    With more pressure applied n/s front would lock up completely. Clearly something has affected the brake balance fairly majorly

    I was planning on taking the car to our agm tomorrow so only have tonight to sort it.

    Can anyone give me any suggestions as to where to start

    Thx

    Paul

  14. Hi Guys

    Thx for the responses

    I haven't rebuilt the O/D and it was fine before reassembly

    I guess off it comes again

    Anyone got any suggestions for keeping the 2 parts of the O/D that the Gbox output shaft slides into aligned as it was a real pig

    Thx
    Paul

  15. Just reassembled the gbox with all the new bits and all seemed to go well, however trying to turn the flange on the end of the overdrive ( that connects to the propshaft) by hand is almost impossible. Is this normal

    Attaching a power drill to the clutch end of the input shaft and sliding the reverse gear into mesh enables the output flange to turn as expected, so all seems to work, I'm just concerned about the amount of effort to turn it by hand

    Opinions please

    Paul

  16. Hi All

    Just about to begin the rebuilding of my '64 TR4 Overdrive Gearbox and want to replace the rear seal which I believe to be at the end of the O/D casing

    My question is whether I have to dismantle the O/D to do this or if I can prise it out without dismantling.

    The O/D works perfectly and so I am reluctant to dismantle.

    Any thoughts please

    Paul

  17. 2-3 years ago I had a problem with my 64 TR4 jumping out of second gear when not under load. After reading the forum and dismantling the Gbox I found the second gear 'Top Hat' bush was sheared. This was duly replaced and all was well with the world.

    Until recently.

    Same problem has re-occured.

    Just had the box out and low and behold 'Top Hat' bush has sheared again.

    Now thinking that sheared bush was effect rather than cause. All the rest of the innards appear fine, no missing teeth or wear marks.

    However the rear gearbox mount has done its usual trick and disintegrated, could this be the cause?

    Anyone got any suggestions what I should check before replacing the bush and refitting

    Also whats the answer to the gbox mount, this will be the 3rd one since I 've had the car

    Thanks in advance

    Paul

×
×
  • Create New...

Important Information

Please familiarise yourself with our Terms and Conditions. By using this site, you agree to the following: Terms of Use.